Leak in fuel supply line causes engine to shut down
- DP Event
- Published on 29 May 2018
- Generated on 24 August 2025
- DPE 02/18
- 2 minute read
Undesired event
Jump to:
A fuel leak developed in a corroded supply pipe to the port main engine. This caused air to be drawn into the system and the engine to shut down.

Comments
The vessel was employed within the renewable energy sector, no details were given of the drilling activities.
A fuel leak developed in a corroded supply pipe to the port main engine. This caused air to be drawn into the system and the engine to shut down.
Redundancy worked as designed. The split fuel system ensured that only the port side of the engine room was affected and operations were suspended due to loss of redundancy.
Considerations
- It was noted that three DGNSS were selected to DP; clearly this is not in accordance with DP equipment class 2 that requires position reference systems to have at least two different principles of operation.
- The vessel was operating closed bus and while the failure did not exceed the vessel’s designed worst case, a different fault on the electrical system may have resulted in a more significant DP system failure.
- Water depth of 45m only provides a small envelope of operation.
- Actions taken in response to the failure appear to be appropriate and in line with good practice.
- The planned maintenance system (PMS) for critical piping systems should be reviewed. For an F.O. supply line to fail due to corrosion should warrant complete inspection of the rest of the system, and a review of past inspections/maintenance so that similar faults are not missed in the future.
Latest DP incidents
-
Always be prepared – Erroneous relative GPS heading input jeopardises follow target operations
Always be prepared – Erroneous relative GPS heading input jeopardises follow target operations
DPE 02/25
1 August 2025
Incident
-
Printer compatibility
This undesired event occurred on a DP Class 3 drillship, whilst operating in open bus configuration and undertaking drilling operations.
DPE 02/25
1 August 2025
Undesired event
-
Inadvertent act causes loss of DP, once again!
While vessel was recovering scrap metal using an ROV and crane, an alarm was triggered, but the DPO could not silence it
DPE 02/25
1 August 2025
Incident
-
Beware the solitons
An equipment class 2 pipelay vessel was engaged in pipelay operations in an area known for solitons
DPE 02/25
1 August 2025
Undesired event
-
DP drill scenario
DP emergency drill scenarios are included to assist DP vessel management and DPOs / Engineers and ETOs to conduct DP drills onboard.
DPE 02/25
1 August 2025
Drill Scenario
The case studies and observations above have been compiled from information received by IMCA. All vessel, client, and operational data has been removed from the narrative to ensure anonymity. Case studies are not intended as guidance on the safe conduct of operations, but rather to assist vessel managers, DP operators, and technical crew.
IMCA makes every effort to ensure both the accuracy and reliability of the information, but it is not liable for any guidance and/or recommendation and/or statement herein contained.
Any queries should be directed to DP team at IMCA. Share your DP incidents with IMCA online. Sign-up to receive DP event bulletins straight to your email.