Case narrative A DP2 platform supply vessel was set up on auto DP engaged in cargo operations inside the 500m zone of a fixed platform. The DP design concept of […]
DP station keeping event bulletins enhance the traditional reporting and analysis of dynamic positioning station keeping events and incidents. They ensure that the industry is provided with prompt feedback, including anonymous factual case studies of events reported to IMCA.
Individual DP events are available individually online, tagged and searchable, while the traditional PDF collections are also available for download.
To be included into the subscription list for the DP Event Bulletin emails, email [email protected]
All members are encouraged to contribute relevant DP information by using our reporting template which is available under Submit a Report where you will also see details on how to submit your information.
Richard Purser
Technical Adviser - Marine
Contact
Case narrative A DP2 platform supply vessel was set up on auto DP engaged in cargo operations inside the 500m zone of a fixed platform. The DP design concept of […]
Comments from the report: The vessel was employed within the renewable energy sector, no details were given of the drilling activities. A fuel leak developed in a corroded supply pipe […]
Comments from the report: The error was traced to a serial interface module for DP Controller A and confirmed that the red error lamp on this module was illuminated. Whilst […]
Comments from the report: During a routine weekly maintenance operation, a ships engineer took an oil sample from the starboard azimuth thruster sample point, which is a small valve located […]
Considerations of the IMCA Marine DP Committee from the above event: Redundancy was lost; therefore, a yellow alert should be initiated. Good practice is to acknowledge and investigate the cause […]
Comments from the report: One of the three frequency converters on the port azimuth thruster was found to be burnt out. Initial actions: The thruster was isolated and faulty converter […]
Comments from the report: A wrongly installed extra capacitor at the bow thruster frequency drive caused overheating of this equipment. The extra capacitor was installed by the electrical designer and […]
Comments from the report: A new gyro was installed as a replacement but failed to start with first attempt. Further investigation revealed that the ‘Gyro 2 remote control unit’ located […]
Comments from the report: The power management system was set for semi-automatic mode as required for DP2 operations. Uncontrolled and unsynchronised closure of the bus tie breaker resulted in simultaneous […]
Comments from the report: The initiating event was the unintentional activation of the DP standby button whilst in Automatic DP control. The radio used to call the installation control was […]
Comments from the report: Initiating event: Inadvertent selection of manual mode whilst in full DP mode Main cause: Human factor – The vessel mode of operation was changed from automatic […]
Comments: Both DGNSS systems had locked up, the touch screen was not responding and the NMEA signal was no longer being received, the DP system alarm displayed ‘Telegram timeout’. The […]
Investigation comments: The DP system reported a thruster pitch prediction error when a large difference between the command and feedback was detected at 20:35:34. The description for a thruster prediction […]
Comments: The event was investigated by the vessel operator, findings are summarised here: Human factors: The DPO was left alone at the DP console during critical subsea operations. In such […]
Comments: At approximately 1555 the ETO came to the bridge and asked the Senior DPO permission to enter the electronics room to check the UPS batteries. The SDPO gave permission, […]
Comments: Various DP equipment, including the DP status lights, were connected via UPS No. 2. Investigation found that the UPS tripped because of a break in the portable cable supplying […]
Comments: The report finding from the vessel concluded: The initiating event was a sudden increase of propulsion to full ahead. The main cause was attributed to the computer with unexpected […]
Comments: Investigation started at the breaker for DG No. 5 in the port switchgear room. The breaker showed tripped and there was a fault present on the auto voltage regulator (AVR). DG No. 5 […]
Considerations from the above event: It is possible that as the vessel was only recently set up on DP, field arrival trials had not yet been completed. The use of […]
Comments It was a single rip tide and when it had passed the vessel was set up back in automatic position mode. There was clear evidence that a degraded performance […]
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