Comments: The report finding from the vessel concluded: The initiating event was a sudden increase of propulsion to full ahead. The main cause was attributed to the computer with unexpected […]
DP station keeping event bulletins enhance the traditional reporting and analysis of dynamic positioning station keeping events and incidents. They ensure that the industry is provided with prompt feedback, including anonymous factual event trees of events reported to IMCA.
Individual DP events are available individually online, tagged and searchable, while the traditional PDF collections are also available for download.
All members are encouraged to contribute relevant DP information by using our reporting template which is available under Submit a Report where you will also see details on how to submit your information.
Richard Purser
Technical Adviser - Marine
Contact
Comments: The report finding from the vessel concluded: The initiating event was a sudden increase of propulsion to full ahead. The main cause was attributed to the computer with unexpected […]
Comments: Investigation started at the breaker for DG No. 5 in the port switchgear room. The breaker showed tripped and there was a fault present on the auto voltage regulator (AVR). DG No. 5 […]
Considerations from the above event: It is possible that as the vessel was only recently set up on DP, field arrival trials had not yet been completed. The use of […]
Comments It was a single rip tide and when it had passed the vessel was set up back in automatic position mode. There was clear evidence that a degraded performance […]
Comments Both the satellite positioning systems in use were from the same provider. The report recognised this and recommended that the systems were changed so that position information was provided […]
Comments After all the checking, it was found that there was water ingress at the L-Band connector to the antenna on the mast. This was dried and cleaned. The connectors […]
Comments Investigation found that the turbo charger on engine No 5 was damaged. DP position was maintained throughout. Considerations from the above event: Sharing information on events such as this […]
Comments The vessel was working in an open water situation and there was no loss of position. Considerations from the above event: Useful reporting of an undesired event that did […]
Comments: A failure of a plug (old decommissioned cooling line for fridge compressors) on seawater cooling pipe for the Ac compressors resulted in flooding in the incinerator room (the water […]
Comments: One of the fans in UPS No 1 failed causing the UPS to overheat and shut down. The fan has been replaced and the temperature alarm tested. Considerations from […]
Comments: During the over boarding of the end termination through the starboard aft chute, the cable laying shift supervisor asked the bridge to isolate thruster No 5 (port quarter) instead […]
Comments: The power plant was configured to work in closed bus mode. No 2 port, No 2 centre and No 2 starboard generator were online. No 1 port and No […]
Comments: The report concluded that the vessel should have proceeded out of the 500m zone to a safe area prior to investigating the fault and conducting tests. Considerations from the […]
Comments: The report concluded that the DPO was conducting too many concurrent tasks so that he did not sufficiently monitor the vessel speed during the time the vessel was being […]
Comments: It was discovered that the 230v supply breaker was open and the uninterruptible power supply (UPS) 2 batteries completely discharged. Warning alarms generated by the DP system regarding the […]
Comments: The report discussed the set-up and mode selection for the thrusters and main engines during high power manoeuvres such as alteration of course and heading. The vessel standing orders […]
Comments: The vessel maintained position throughout. The ROV was restricted to the tether management system (TMS) until the vessel was confident of the cause of the thrusters’ unexpectedly stopping. All […]
Comments: The vessel maintained position throughout. The lift had not been properly planned or risk assessed for the object being lifted. There was a failure to recognise that the mattress […]
Comments: The bow thruster gave an alarm that pitch was at maximum showing 114% on DP display. Investigation concluded that the full starboard maximum limit command/set point of the bow […]
Comments: The seat for the stop solenoid on the port main engine was damaged causing a slight air leak past it, this acting on the stop cylinder piston caused a […]
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